Could well be, they seem to be susceptible to air leak related problems. Either way it needs replacing and if it cures some of your woes that'd be a bonus.
Tony.
Tony.
Hi ya, yup MAF still in place, cleaning the injectors and replacing the vacume pipes attached to them was the best fix. There is a good thread on M44 injector cleaning which shows the pipes, I bought a length of fuel pipe to replace these small pipes with from the same shop, can't remember the bore tho. The PCV valve tubing was shot from the inside out, if you squeeze it & it is slow to return to shape have a look at that.. Most of this stuff is visble if you take off the top inlet manifold. if you do the injectors be careful when you vent the fuel out of the valve on the injector rail, do it with a cold engine & lots of rags to soak up the fuel. Or follow the book & remove the fuel pump fuse & run the engine till it stalls.
https://zroadster.org/articles/m44b19-fuel-injector-replacement.76/
good luck
Any chance you are using Tapatalk? There is a bug they were supposed to have fixed with links in their app. Try accessing the site using a web browser, and you will have a much better experience....Canman and motor neurone disease........ that's what I get when I click the link![]()
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I think this is going to be the plan, but first I have error codes on the knock sensors. Going to replace them first then if that's ok straight for the k&n. I put one on my e46 was impressed with the extra milage I was getting. [emoji108]. (Ohhh how you doing) I look nothing like joey by the way [emoji23]
Possibly in theory but due the great sound under load I have always seen consumption plummet after exhaust/intake mods!Do you get improved MPG then with the K&N kit ?
Do you get improved MPG then with the K&N kit ?
Glad you are slowly taking care of those niggles, just be patient and soon the zed will be what you want. Then you'll get the " what can I do next" syndrome and make it truly yours. JIMI had one on my e46 not a induction just the flat k&n and yes imdefo got better milage not a great deal but according to the trip computer I was getting a extra 4-6 mpg.
Got back under the bonnet today and the plug I found was the actually the knock sensor so found where to plug it in and so far it's not popped up on the code reader so another job down.......
Now my dials work intermittently (shake my head lol)